Reducing Non-Productive Time (NPT) In The Seven Well Drilling Project On The North Beach Of Javafrom PT Multi Jaya Tehnik
Abstract
Oil and gas as fuel are still the main needs for human needs on energy, and to
obtain oil or natural gas, the drilling process should be executed. The drilling
process is an expensive investment and requires a very high cost. Drilling cost is
critical factor in determining the financial returns from an oil and gas
investment. One of the factors that determines the cost efficiency of drilling is
reducing the Non-Productive Time (NPT) or downtime. Downtime is an
undesirable outcome in any operation. The NPT makes the high cost of drilling
process. The higher the NPT,the more expensive the drilling costs will be.
Drilling optimization is the key to reduce Non-Productive Time /NPT. There are
many factors that cause NPT include natural factors, technical factors, human
resources, and availability of equipment. For this reason, this study will examine
the NPT in the drilling project undertaken by PT Multi Jaya Tehnik (MJT).
This research is a quantitative study with cross sectional method which was
carried out on 7 oil drilling projects by PT MJT. The data collection was carried
out during the internship in July 2019.
The research finds that from the 7 well drilling projects of PT. MJT, the result
shows from the total operational time, how of 4.144,76 hours is lost due to NPT,
of which 2420,25 hours is NPT ER.
By reducing NPT via various means on focus of the equipments which PT. MJT
provides, the projects can reduce loss time caused by NPT noticeable while also
improving PT. MJT quality of service as an equipment rental company.
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